Thursday, November 5, 2009
Where has the time gone?
Thanks for being patient.
Sunday, October 4, 2009
I could use a thousand words or.....


To make a 3DP I needed to not only automate the "reset" but also, precisely control the movement of 2 bins, switch a dc motor on an off, and be able to tell the printing computer to "wait" and not send the next page until the printer is ready. I could have built a dedicated circuit to do all this but as I stated earlier, My knowledge of electronics is limited and I don't have a clue how to program a PIC. I decided instead to go with a CNC setup. The inkjet still does all the actual printing then the CNC takes over and re setts the gantry, adjusts the powder bins,spreads the powder, and then tells the printing computer that it can send the next page. You can see in the diagram that PC 2 has replaced the pulse generator and a relay has replaced switch 2. Additionally, 2 more steppers and a 2 axis stepper driver have been added. Switch 4 gives feedback to the control program and signals the change from the print to the recharge cycle. Relay 2 breaks the connection on pin #11 of the inkjet's parallel port. this tells the PC that the printer is "busy" so it wont send another page until the printer is ready. Relay 3 is connected to the motor that runs the powder roller. The breakout board is a convenient place to make all the connections to the parallel cable and PC 2. Note that the parallel port of the PC doesn't output enough current to drive a relay directly so I used the outputs to switch transistors that supply 5v to the relays.
For the CNC control I use TurboCNC and a G-code program. The program is a step by step set of instructions which can be used to set the logic state (high/low) of the parallel port pins. Also, pins can be monitored and step pulses can be sent to the stepper drivers.
Hopefully this helps clarify what I've done. If I haven't answered your questions feel free to ask.
Wednesday, September 23, 2009
Time to get back to it.

Wednesday, September 9, 2009
“It cuts though a tin can then slices a tomato!”
The utility is easy to use and doesn’t require any additional programming skills. Simply open your stl file in the slicer, pick a printer, set the slice thickness, and hit print. You can scale and rotate the model as well as shift the print position to center it on the page. One thing to note is that the measurements are in metric. You need to convert your stl to millimeters if you want it to print at the size you are expecting. My other observation is that the mesh must be clean and watertight. From what I understand, that’s not unusual for 3D printing. It’s probably also the reason the other software was so expensive. Unfortunately, my meshes are typically neither clean nor watertight (I really need to learn better 3D modeling skills).
I am modeling in Silo and using MeshLab to check and repair my meshes. Some are so hopelessly messed up that I’ll have to go back and start over. (There is also a slice feature in MeshLab but it outputs svg outlines and I need silhouettes.) MeshLab is open source and can be found at Sourceforge (http://sourceforge.net/projects/meshlab/). Silo is available from Nevercenter (http://www.nevercenter.com/about/) for a modest $99 ($159 for the pro version). They have a 30 day trial if you want to check it out and a very friendly and helpful users community. I'm still very much a Noob with Silo but I found it to be much more intuitive than Blender and WAY less expensive than Rhino, Lightwave, or any of the CAD packages (Hell, even Google Sketch Up is like $495 if you want to be able to output anything other than their own format). Again, if this wasn't a hobby (and I wasn't incorrigibly cheap), expese wouldn't be such a big issue.
Anyway, now I need to make my repairs and whip up some test files.
Monday, September 7, 2009
Lather, Rinse, Repeat
Oh Noooo!!!!! Somewhere around layer 170 one of the belts came loose! I'm going to have to come up with a more secure clamp. Once I get the belts fixed I'll be ready to try again. For now I'm trying to use up the ink in a new cartridge. I tried to refill an old one with the water/vodka mix but it was hopelessly clogged. I figure I'll have better luck with a new one. For now I'll keep working on getting the powder layer as smooth as possible. I also need to install a limit switch on the supply bin so it stops when it reaches the top.
Thursday, September 3, 2009
Some Assembly Required
Welcome to The Pit of Despair!


